I seem to have broken my motor mount, the head sheared off.
On the bolt head, it is marked 10.9 so I think it should have been a good bolt.
I broke it being stupid, with sticky tires and a 3,000 rpm clutch drop from a stop.
Looking at the mount, I think it is designed to hold the motor down when the axle is trying to wind it up. It looks like a straight tension bolt that has been overloaded. With enough torque and enough hard launches, I fear it will fail again.
I'm going to order a new mount and then see if I can figure out a way to modify the mount for a larger fastener.
Oh, Cobb stage 1 OTS tune, K&N filter, Mountune intake hose.
I'm going to check out my CV joint boots too.